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dc.contributor.authorAslan, Sukru
dc.date.accessioned2019-07-27T12:10:23Z
dc.date.accessioned2019-07-28T10:15:51Z
dc.date.available2019-07-27T12:10:23Z
dc.date.available2019-07-28T10:15:51Z
dc.date.issued2008
dc.identifier.issn0378-4738
dc.identifier.urihttps://hdl.handle.net/20.500.12418/10482
dc.descriptionWOS: 000252744100012en_US
dc.description.abstractThis research evaluated removal of nitrates from drinking waters in a slow sand filter (SSF). Batch experiments were performed to determine optimum carbon to NO3-N (C/N) ratio for the filtration experiments. The filter column was filled with filter sand of an effective diameter of 0.5 mm and uniformity coefficient of 1.23. The filter was operated at filtration rates of between 0.02 to 0.120 m/h and 0.01 to 0.25 m/h with concentrations of 22.6 and 45.2 mg NO3-N/l, respectively, and effluent samples of the SSF were taken at 6 depths of 10, 15, 20, 40, 60, 80 cm, and the bottom. Optimum C/N ratio was found to be 1.5 when using ethanol in batch tests when the removal efficiencies of NO3-N and C were higher than 90%. Although increasing filtration rates decreased NO3-N removal, effluent NO3-N concentration at the effluent port of the SSF was lower than the limit value. Most of the NO3-N removal was carried out at the upper layer of (10 cm) the filter bed. Concentration of NO3-N, NO2-N, and C were not detected at the 60 cm depth of the SSF through the study for the inlet concentrations of 22.6 mg NO3-N/l. As expected, increasing influent NO3-N concentration to 45.2 mg/l increased NO 3-N, NO2-N, and C concentrations in the effluent water. The SSF process was unable to provide NO3-N removal rate of more than 228 g N/m(3) center dot d (0.2 m/h flow rate, 217g N/m(2)center dot d of surface loading rate). The NO 3- N removal efficiency dropped slightly from 96 to 95% when the loading rate increased from 228 to 285 g/m(3) center dot d, but the effluent water contained higher concentrations of NO2-N (8.4 mg/l) than the standard value. The results of the SSF experiment demonstrated that averaged nitrogen conversion to volatile solids was about 0.77 mg VS/ mg NO3-N.en_US
dc.language.isoengen_US
dc.publisherWATER RESEARCH COMMISSIONen_US
dc.rightsinfo:eu-repo/semantics/openAccessen_US
dc.subjectbiodenitrificationen_US
dc.subjectslow sand filtrationen_US
dc.subjectdrinking wateren_US
dc.titleBiological nitrate removal in a laboratory-scale slow sand filteren_US
dc.typearticleen_US
dc.relation.journalWATER SAen_US
dc.contributor.departmentCumhuriyet Univ, Dept Environm Engn, TR-58140 Sivas, Turkeyen_US
dc.identifier.volume34en_US
dc.identifier.issue1en_US
dc.identifier.endpage105en_US
dc.identifier.startpage99en_US
dc.relation.publicationcategoryMakale - Uluslararası Hakemli Dergi - Kurum Öğretim Elemanıen_US


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